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Evidence of landslide activity at the site was initially observed in 1977 shortly after construction of the roadway. Repair of the landslide was classified as an emergency due to the threat of road closure and the probability of accelerating movement if left unattended. An earthen berm was recommended for stabilization of the slide due to the simplicity of construction and ease of developing plans. The berm required approximately 175,000 cubic yards of fill and the acquisition of approximately 10 acres of additional right-of-way.
BCD recommended a permanent ground anchor/buried anchor block stabilization system. This system was constructed without acquiring additional right-of-way, without impacting existing high pressure gas lines, and was contracted and constructed in a relatively short time frame.
Role of Other Consultants
MDOT completed soil borings, installed geotechnical instrumentation, and made geologic interpretations of the subsurface. ABMB Engineers, Inc. performed the land survey. Advanced Engineering Resources served as structural engineer for the project. Hayward Baker, Inc. (HBI) was the specialty geotechnical contractor. HBI provided the Original and Innovative Applications of New or Existing Techniques
Geologic interpretations of soil boring and downhole geophysical data revealed an extremely complex system of progressive landslides. It is postulated that landslide activity began in the late Pleistocene epoch (10,000 – 20,000 years B.P.) and failure progressed from west to east. Sliding was most likely triggered by degrading of the valley west of the landslide by Hennesseys Bayou. The majority of the slide plane was found to be in high plasticity clays of the Catahoula and Bucatunna formations. Instrumentation installed and monitored during this investigation revealed that the velocity of the slide is proportional to groundwater levels. Several constraints had to be considered in the selection of a stabilization system: 1) It was important that the system be designed and constructed in a short time frame. Large movements of the landslide could threaten the northbound lanes and would result in increased costs for reconstruction of the southbound lanes; 2) The stabilization system needed to be confined to the existing right-of-way. The acquisition of additional right-of-way would result in significant time delays and expense; 3) High pressure gas lines located just west of the toe of the slide could not be impacted by construction; 4) A residence is located within the limits of the landslide south of the existing right-of-way; and 5) Topography in the project area is relatively severe and limits alternatives for new alignment of the roadway. A number of possible methods of repair were considered. These included realignment of the roadway, lowering the grade of the southbound lanes, subsurface drainage, a drilled shaft retaining wall, an earthen berm, and permanent ground anchors. Permanent ground anchors were selected based on cost and conflicts of the other options with the constraints described in the preceding paragraph. The design resulted in five rows of anchors evenly spaced from the crest of the slope to the toe of the slide with an anchor capacity along each row of 25 kips per foot. The anchors were bonded in limestone layers within the Glendon formation which underlies the high plasticity clays. At the surface, each anchor was attached to a reinforced concrete anchor block dimensioned to limit the contact stress between the anchor block and soil to 2,500 lbs per sq ft. The anchors were inclined at 45 degrees from the horizontal. Anchor lengths ranged from about 250 ft to 115 ft. The design capacity of each anchor was 465 kips. A total of 250 anchors were installed with a design capacity of 465 kips per anchor.
The anchors basically consist of high strength cables grouted into a borehole. Each anchor includes a bonded zone and an unbonded zone. Within the unbonded zone, the cables are greased and encapsulated in plastic sheaths to prevent bonding to the grout. The cables are in direct contact with the grout in the bonded zone. Grouting is accomplished by pumping through a tremie tube that is bundled with the cables and extends to the bottom of the borehole. Two levels of corrosion protection are provided – first by the grout and second by a corrugated plastic casing extending the full length of the anchor. Every anchor was load tested to verify capacity. After testing, the tension in the anchor was “locked off” by means of wedges at the head of the anchor. The load in each anchor was also measured 28 days after “lock off” to determine whether any de-tensioning had resulted due to settlement of the anchor block. Groundwater levels and ground movements were closely monitored during construction. Construction sequences were adjusted to minimize ground movements. Future Value to Engineering Profession Social, Economic and Sustainable Design Contributions Complexity Exceeding the Owner/Client Expectations
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